The thrust levers were advanced, the first officer selected the go-around mode for the flight director, and he started to increase the pitch of the aircraft to the command bar indications, 10 degrees nose up. About one second after the first officer acknowledged the go-around, the stick shaker (stall warning) activated. As the aircraft reached 10 degrees nose up, about one and one-half seconds after the stick shaker activated, the captain called flaps and selected them to the go-around setting, the warbler tone associated with the stall protection system (SPS) sounded, and the aircraft stalled aerodynamically. The aircraft rolled right to approximately 55 degrees of bank, and the right wing tip contacted the runway about 2700 feet from the threshold and 45 feet left of the centre line, the right wing tip bending upwards about four feet from the tip.